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No. 4 "The Chief" |
The ChiefThis page details the modifications made to No.4, The Chief. These were all been carried out one at a time as experience with the engine grew and after visiting shows where other engines were seen running. The first of the alterations was simply to apply the number and name plates, then the tank side lettering and lining. The steam whistle was next and the operating lamp followed quickly. A very nice simple addition was the brass safety valve cover which just sits over the existing safety valve. Loco running lamps (as opposed to the searchlight) were bought and hooked onto the supplied brackets on the bunker, a bracket was added to the front footplate for that lamp. The front buffer beam and water filler are the latest additions. Name and Numbers Numerically, this loco was always going to be number four, since it was the fourth on the line. That makes sense, and the name came easily too, since the funds to purchase the Lady Anne came from my fathers legacy; he was a Chief Engineer with BP Shipping until he retired. The name and number plates were ordered from MDC via Brandbright, and are really good quality, although you may have to wait a while for delivery. They have been attached using Cynoacrylate (Superglue) in very sparing amounts, great care been taken to ensure they are straight since in this application the glue will set immediately. Lining
Steam Whistle This was the first major addition to the loco which involved dismantling. The kit of parts I assembled before starting was as follows:-
Removal of the bodywork was simple, two bolts under the leading edge of the side tanks and two nuts under the rear of the cab. Once clear, I could determine where the whistle would sit and how to mount the servo. The location of the valve was then apparent from the servo linkage and the stiffness of the pipe work meant that no other mount was needed. I removed the lubricator and pipe work from the loco and cut the pipe between the regulator and lubricator. The tee was soldered into place here and a short length of new pipe run from there to the whistle valve. I then fixed the lubricator back in place and fitted the whistle into the left side tank alongside the reverser servo. The whistle exhausts downover, to prevent it filling with condensate. Next the servo was fitted on an L bracket to the floor of the cab and the servo horn connected to the whistle valve. The third channel on the radio was used for the whistle servo at first, then I swapped it for channel one, since the reverser is usually held in full gear either way, the spring on the stick being redundant. I have since added a two way centre off switch to channel three so that I can select forward or reverse easily. Searchlight The working headlamp was bought at a show and has a 12v incandescent bulb
fitted. Running from a 9v PP3 battery, this gives a good oily glow. The lamp is
fitted to the smokebox top with a single self tapping screw in a hole drilled
just forward of the chimney. The power is fed to the lamp via a 1/16" copper
tube with a single PTFE coated wire core. The tube itself is the -ve supply, the
wire +ve. The battery is mounted in the right-hand tank above the radio receiver
and a spare radio power switch is used to turn the lamp on and off.
Drop-Links A simple but effective accessory from R/H were these dummy Walschearts drop links. They look wonderful when the engine is moving slowly past. Added by removing a screw and a bolt, then replacing with the new bolt and screw provided by R/H. Buffer Beam
Water Filler
Spektrum and a Clean After around eight years of sterling service, the arrival at the CSLR of a Spektrum radio control set prompted a bit of a clean and polish of The Chief whilst replacing the radio receiver. As with such exploits, the strip down was used for a couple of other changes too.
At some time during travels, the plate to which the smokebox is mounted had become distorted, so it was necessary to remove the boiler, 'box and this plate in order to flatten it. With the loco stripped this far down, an extensive degrease, de-gunk and de-muck was in order, reaching those parts that you usually cannot reach.
September 2007. A pronounced clanking at a recent show turned out to be worn big-ends. To fix this is not a simple job as the return cranks need to come off, and these are pinned in place during manufacture to ensure the timing stays put. However, in order to make the job 'a good un', I've replaced the axles and their bushes (since they too showed considerable wear) and a set of replacement coupling and connecting rods, complete with crankpins sits before me on the workbench.....
The replacement rods have been fitted successfully, the smoothness of operation is returning as The Chief is run in once more. The Warley Show returned a succession of 35 minute runs with ease, only topping the water to compensate for the amount of whistle blowing! The Chief also now sports Accucraft chopper couplings front an rear, giving a more prototypical appearance. Needs a little red paint on the front buffer beam now. |
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